The EV1 is currently having a next generation Ballard Integrated PowerTrain (IPT) fitted and installed. We're currently fabricating new motor mounts and they will soon be welded into the frame. Once the mounts are welded and the wiring installed we'll be recieving a new IPT from Ballard to test in the EV1.
Back Story
What do you do with 50 undergraduate
students in the first year of a
vehicle competition that is strictly
modeling? Find a vehicle for them to work
on! Wisconsin received an EV1 from
General Motors (GM) when they were in the
process of dismantling and recycling them at
the end of the EV1 lease program. GM generously
donated disabled EV1's to any university
that requested one. In addition to
removing the high voltage batteries, GM
had removed the main drive controller, the
power steering pump controller, the brake
controller and the body controller - they
intended the vehicles to be looked at and
studied, but never driven.
So in a year when most Madison students
would have turned their interest to a favorite
Wisconsin pastime - BEER, a special group
of engineering students took on the challenge
of reincarnating our bright red EV1.
This task would be as difficult as building a
hybrid while offering new challenges to the
students. This would be the first time they
would be working on a charge-depleting
vehicle - let alone a fully electric one.
Several veteran hybrid team members started
the project in September of 2004. With
no place to store or display the EV1, the
rally cry was "fix it or scrap it".
The first
feat was creating a 380 volt battery pack.
The original battery pack mounted between
and behind the two seats creating a large T-shaped
battery box. Removing the battery
tray the first time was easy since the batteries
had been removed before delivery. Upon
inspection of the battery tray, one of our students
had an idea. They proceeded to the
battery room and retrieved a nickel metal
hybrid battery originally used in the electric
Ranger project that had since been donated
to our university by Ford Motor Company.
THE BATTERIES FIT - General Motors
had actually used an industry standard battery
casing. With much anticipation, all of
the batteries were uncrated and hauled from
the battery room to the garage. This took
awhile, as each battery weighed approximately
80 lbs. But wait, we were SIX batteries
short - now what? Could we order
them? Sure, but they were $2800 each and
you have to order a minimum of 26. That's
$72,800 - OUCH!! After a significant
amount of brainstorming, Wisconsin contacted
our counterparts at the University of
West Virginia (they were one of about 6 universities
to have received the batteries
through the Ford donation) to see if we
could purchase six precious batteries from
them. To our surprise, the Mountaineers (West
Virginia school mascot) donated the batteries
to the Wisconsin reincarnation project.
Now we had a complete 95 amp-hr nickel
metal hydride pack - this equaled the capacity
of the best EV1 that General Motors had
produced.
The next major component that needed to be
replaced was the motor controller.
Wisconsin had a spare Solectria DMOC 445,
the same controller that is utilized in our
2004 FutureTruck to drive an identical EV1
motor. The only drawback was that the
Solectria was rated for 78 kW and the motor
was rated for 105 kW - Tim Taylor (of Home
Improvement fame) would not be happy, but
Wisconsin decided that it was our only alternative.
After mounting the controller and
adding the appropriate speed pick-up to the
original motor in the EV1, we were abruptly
disappointed as the controller only made the
motor hum and shake. Upon contacting
Solectria and giving them the model number
of both controllers, we were informed that
the control boards were 4 revisions apart and that they
did not know how to convert the calibration
parameters from our FutureTruck controller
into the one in our EV1.
Frustrated and in disbelief, the team was
forced to put the EV1 project on hold.
Without a motor controller, the EV1 reincarnation
was stalled. Then, while working
with Ballard Power Systems to arrange for
the purchase of an IPT (Integrated
Powertrain) for our Challenge X program,
Ballard graciously offered another
Integrated Powertrain to Wisconsin as a
heart transplant for our EV1. This was a
great first step as it was the same unit that
would ultimately be hybridizing Wisconsin's
Challenge X vehicle.
However, using the Ballard unit posed ONE
LARGE mechanical hurdle - the suspension/
motor sub-frame had to be drastically
modified. The original EV1 powertrain
mounted the motor above the sub-frame and
used an in-line gear reduction to transfer the
torque below the motor where the axle
shafts connected. Since the Ballard unit utilizes
a hollow shaft motor with planetary
gear reduction and differential, the subframe
would have to be widened so both
would fit inside.
The Wisconsin Hybrid team had experience
in aluminum structures as they have created
3 different aluminum truck frames in the
last 5 years. Using stiff, heavy pieces of
steel, the students created a welding jig that
bolted to all the sub-frame's critical mounting
points. Next, they took a perfectly good
sub-frame and cut it into 3 pieces! The new
design lowered the sub-frames axial members
to be below the main A-arm mounting
point while the cross member that holds the
steering rack was left in its original location.
After adding several stiffeners and adding
towing points to the sub-frame, the IPT was
lowered into place.
Meanwhile, the controls group was rewiring
the vehicle and re-engineering the logic for
the controllers that had been removed
before delivery. In particular, the rear
brakes are activated using a ball-screw actuator.
Besides having to engineer the Hbridge
driver for the motors, calibration
between brake pedal position and braking
resistance had to be correlated. They also
programmed a PIC micro-controller to control
the dash, security and HVAC. After the
IPT was installed, a Freescale MPC 555 was
integrated into the vehicle as the interface
between the driver's request and the IPT.
With everything checked and doublechecked,
it was time to try to spin the
wheels!!! To our dismay, we couldn't get
the IPT to 'wake-up'. Although Ballard had
been overly helpful in answering all of our
technical questions in a timely manner, this
problem could not be solved via email or
phone calls. After trying for several days, it
was time for a road trip. We loaded the EV1
into our rig and headed to Ballard Power
Systems Inc. located in Dearborn,
Michigan. The trip had a double purpose as
we were also attending SAE International
Congress. While at Ballard, we discovered
that we had installed the IPT backwards!
Since the IPT utilizes a mechanical oil pump
(no lubrication while spinning in reverse), it
wasn't as simple as reversing the control
logic. A quick look on the CAN bus
revealed an incorrect software version on
the IPT controller and a record length error
on a CAN message. After a couple of memory
stick file exchanges, an IPT reflash, and
a quick update on the EV-1 code, the unit
was up and running. The EV1 moved under
its own power and the reincarnation was
almost complete.
We returned to Madison with a bittersweet
victory: the EV1 lived but required the
reversal of the IPT. During April and May,
the team worked hard to correct the orientation
of the IPT, incorporated some suggestions
provided by Ballard and finalized the
wiring and EV1 controls.
In August of 2005 Wisconsin's Hybrid Team
returned to Ballard Power Systems for a
final checkup. After several hours of testing
and diagnosis, the EV1 was given a clean
bill of health. Since then, it has operated
flawlessly providing invaluable data to the
Wisconsin Hybrid Team while educating
our next generation engineers. The EV1
project is another example of the dedication
and creativity of the young engineer's mind.
This small group of undergraduate students
has and will continue to make important
contributions to the advancement of personal
mobility.
Videos
Chevrolet Suburban
RIP
The Hybrid Vehicle Team utilized a Chevrolet Suburban for the first two years of the Future Truck Competition. The surburban was nicknamed the Moolenium, it ran a diesel engine with B20 Biodiesel and an electric drive.